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Failed mast-based launch attempt of the V3 kite

Formale Metadaten

Titel
Failed mast-based launch attempt of the V3 kite
Untertitel
Video recorded on 2 August 2012 with a GoPro camera on the ground next to the launch mast
Serientitel
Anzahl der Teile
15
Autor
Mitwirkende
Lizenz
CC-Namensnennung 4.0 International:
Sie dürfen das Werk bzw. den Inhalt zu jedem legalen Zweck nutzen, verändern und in unveränderter oder veränderter Form vervielfältigen, verbreiten und öffentlich zugänglich machen, sofern Sie den Namen des Autors/Rechteinhabers in der von ihm festgelegten Weise nennen.
Identifikatoren
Herausgeber
Erscheinungsjahr2020
SpracheOriginalton ohne gesprochenen Text
Produzent
Produktionsjahr2012
ProduktionsortFormer naval airfield Valkenburg, Leiden, Netherlands

Inhaltliche Metadaten

Fachgebiet
Genre
Abstract
The video recording shows a failed launch attempt of the TU Delft V3 kite from an upside-down hanging position on 2 August 2012 at the former airfield Valkenburg, Leiden, Netherlands. The GoPro camera is placed on the ground next to the launch mast. As for all previous mast-based launch attempts, the hanging kite is first steered into a pendulum motion, before taking off with a sideways upswing maneuver to the right. This upswing motion ends at the side of the wind window with a roughly horizontal tether and the kite subsequently falling back. A possible contribution is the sudden drop of the propulsive aerodynamic force, which is indicated by the observable loose membrane and partial collapse of the entire right half of the wing. While falling back, the kite again catches wind and regains power, and this time is steered into a sideways upswing maneuver to the left. Towards the highest point above the mast head, the kite slows down and, unable to sustain a stable flight mode, accelerates into a sideways downswing maneuver, crashing into the line suspension system of the launch mast, however, staying fully intact. Only a few seconds later, the hanging kite regains speed and is steered into a similar upswing-downswing maneuver, again crashing into the line suspension system. This crash is slightly harder, deforming the entire wing, which then recovers and performs a smaller final loop before again crashing into the line suspension system, where it then comes to a rest. This launch was also covered by data recording, by a regular photo camera and by a second GoPro video camera, that was taped to the rear side of the leading edge tube of the wing, between the two center struts, looking at the kite control unit. Because the time of the GoPro video camera was incorrectly set, we used the short initial pendulum motion of the hanging kite as a clearly identifiable event in the video and the data recording to determine the correct starting time of the video, 20:32:01, which was then set in the video metadata.
Schlagwörter